Station:
- A 400MW single-shaft combined-cycle plant, including a 150MW three-pressure HRSG with reheat
Problem:
- Irregular movement of a reheater header at maximum load, with potential for reduced fatigue life of tube-to-header welds
Approach:
- Team approach with the prime contractor, OEM and operator
- Design review; plant instrumentation and monitoring
- External observation during operation; internal inspection off-load
- Investigation of the effect of operational parameters
Benefits:
- Flow induced vibration of tube-bank identified as prime cause, being predicted to generate displacements and frequencies comparable to those observed
- Addition of tube spacers implemented, leading to elimination of problem and allowing operation at full power to be resumed
- Secondary effect of attemporator performance identified as requiring further investigation
Publication:
Brear, J.M. and Jarvis, P.
“Tracing a vibration problem back to source”
ETD Int Conf ‘Heat Recovery Steam Generator Technology’, Woburn House, London, 10-12 Nov 2003